In Chaves County, NM, 55 shallow wells faced paraffin, scale, and emulsion issues, causing high costs and instability. Installing Avenger rod pump tools reduced paraffin, improved uptime, and cut costs. By January 2023, 40% of wells had Avenger tools, with the operator calling it a game-changer.
A Pacific Basin heavy oil producer faced severe wax buildup, causing instability and high costs. Installing Synergetic’s technology eliminated wax, reduced rod loads by 25%, and stabilized production. Improved viscosity and flow confirmed its effectiveness, making it a game-changer for heavy oil operations.
Diamondback Energy faced severe paraffin buildup in Upton County wells, causing downtime and high costs. A three-month trial of Synergetic’s Enercat Tube reduced paraffin, extended well run time, and eliminated chemical treatments. Success led to broader adoption, improving efficiency and cutting expenses.
Devon Energy’s Cotton Draw Unit wells faced severe paraffin issues, causing downtime and high costs. A 130-day trial of Synergetic Enercat Tubing Tools reduced paraffin, eliminated treatments, and ensured clean flowlines. With uninterrupted production and cost savings, the technology proved to be the best paraffin prevention solution.
A Kansas Mid-Continent producer installed Synergetic Downhole Tools in 22 stripper wells to combat paraffin issues. Over two years, the tools eliminated chemical treatments, boosted production by 39.3 BOPD, and cut costs. With over $1M in added revenue, Synergetic proved a highly effective long-term solution.
A Delaware Basin oil producer faced severe paraffin buildup, causing downtime and high costs. A 130-day trial of Synergetic Downhole Tools reduced paraffin, kept flowlines clean, and cut chemical costs. With uninterrupted production and lower maintenance, the results exceeded expectations.